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PollyMobiles Rebuild

Removed the used shaft

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Trying to insert the inner CV joint into the gearbox was a PITA, unable to push it in.
Turns out they use this short kinked clip which pokes outside the spline too much and jamming the insertion.
Swapped it with the regular round C-clip instead

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Installed & working nicely, there's almost no sloppy movement in the shaft :cool:(y)

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The next thing to fix for the Porsche Spyder were some bushings for the gear selector shaft

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there was surprisingly only 1 bushing per tube (one near the gear stick and the other underneath the engine) and they were seriously worn out

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there's 2mm gap from the 18mm selector shaft! :unsure:

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ordered some nylon

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cut to length

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machined the outer groove & 18mm hole

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2 new bushings fitted

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now the shaft is supported with minimal play :cool:

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While cleaning the house, I gave these old BBS wheels a little jet wash, really need to sell these off to make room :sneaky::sneaky:

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I measured the spare driveshafts and damn it Nissan, why did they have to use soo many different splines? 🤨

Inner CV = 24T, 23.30 - 25.60mm
Driveshafts = 22T, 22.50 - 24.30mm
Outer CV = 23T, 22.10 - 23.80mm

I was hoping to use the broken left driveshaft to slot into the LSD for checking the LSD preload but the splines don't match. I'd have to sacrifice two inner CV joints instead 🙄

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Recently on ebay I ordered some 40-56mm driveshaft oil seals to fix the leaking gearbox but received some smaller 25-40mm seals instead 😒

Tday after contacting the seller they said keep the incorrect item & I received the correct 40-56mm seals, but curiously I wondered if the smaller seals fit the input shaft? 🤔

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ooh they do! 😃
so basically I purchased 2 driveshaft oil seals & got a pair of input shaft seals for free too 👍

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Stripping apart the spare power steering rack, which I converted into a manual rack yrs ago, to reattach a missing part

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This rotary valve sleeve needed to be attached to keep the pinion in place (when it was previously missing, the pinion would jump off the bearing during right turns)

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Covering the bearing surfaces

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Welded the sleeve onto the shaft

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Assembled & ready to try out someday

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The next thing to fix for the Porsche Spyder were some bushings for the gear selector shaft

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there was surprisingly only 1 bushing per tube (one near the gear stick and the other underneath the engine) and they were seriously worn out

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there's 2mm gap from the 18mm selector shaft! :unsure:

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ordered some nylon

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cut to length

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machined the outer groove & 18mm hole

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2 new bushings fitted

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now the shaft is supported with minimal play :cool:

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Great work Paul. If you do bushes like that in future consider using 'Nylatron' instead of 'Nylon', it has far better wear properties..... https://www.mcam.com/en/products/shapes/engineering/nylatron-ertalon
 
checking the car over before the Unity Car Show, I noticed the throttle cable was slightly loose & didn't open WOT fully therefore during the recent datalog footage the TPS wasn't reaching 4.2kOhms, which might have affected the recent dyno results at santapod :unsure:

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the drivers door kept getting water stains and I figured the garden hose was leaking & dripping onto it 😒

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polished the stains away

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added some extra stickers to balance out the boot decorations lol 👀🫣😅

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the adjustable gear stick mount kept shaking loose so I redesign it

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rather than making a split adjustable ball-joint case, I match the original design but tailor the size of the insert to match the ball size

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mounted the new casing over the ball-joint insert for a snug solid fitment

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2024-08-25 Unity Car Show

6am left to meet up with the convoy in Thirsk

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arrived at a sunny NY500 cafe.
compared to previous years, this one was rescheduled from a wet March & with other shows happening elsewhere it was really quiet, not as many ppl turned up

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removed the strut brace containing the PAS hoses

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bit more room without all that plumbing

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removed the tie-rods

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disconnect the column joint

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removing the bulky PAS rack required lots of wriggling

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power steering rack vs manually converted rack

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fitted the manual rack but frustratingly whilst turning the wheels on the ground, the pinion once again kept clunking up/down by 5mm & popping this plastic dist cap off.
I'm sure I welded the rotary valve in the right spot :unsure:

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but looking back, what I previous thought was just a dust cap turned out to be a load bearing threaded cap which keeps the ball bearing secured to the rack to resist the pinion shaft thrust forces

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so I machined a new cap

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screwed on and now it doesn't clunk anymore and feels solid & secure :cool:

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aligning the steering joint to the pinion splines so the steering wheel has equal amount of turns lock-lock

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tied the throttle cable & loose loom out the way, ready to test drive

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during startup, the throttle cable was slightly sticky so I rerouted it better



steering was obviously very heavy under 5mph, especially when turning lock-lock out the garage, leaving T-junctions & going slowly at roundabouts where the LSD engages, requiring slight change in driving habit.

5-30mph the steering weight felt normal.

at high speed the weight feels light, very responsive feedback during turn-in (great on track) but during mid-corner the wheel starts to feel slightly heavy under the cornering forces, especially when accelerating & the LSD locks up.

she also feels rather nippy.
dunno if it's the conditions, placebo effect, reduced weight or less hydraulic drag from the deleted power steering pump providing more HP to the wheels :unsure:
I'll be curious to see if this also improves mpg too.
 
removed the strut brace containing the PAS hoses

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bit more room without all that plumbing

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removed the tie-rods

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disconnect the column joint

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removing the bulky PAS rack required lots of wriggling

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power steering rack vs manually converted rack

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fitted the manual rack but frustratingly whilst turning the wheels on the ground, the pinion once again kept clunking up/down by 5mm & popping this plastic dist cap off.
I'm sure I welded the rotary valve in the right spot :unsure:

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but looking back, what I previous thought was just a dust cap turned out to be a load bearing threaded cap which keeps the ball bearing secured to the rack to resist the pinion shaft thrust forces

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so I machined a new cap

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screwed on and now it doesn't clunk anymore and feels solid & secure :cool:

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aligning the steering joint to the pinion splines so the steering wheel has equal amount of turns lock-lock

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tied the throttle cable & loose loom out the way, ready to test drive

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during startup, the throttle cable was slightly sticky so I rerouted it better



steering was obviously very heavy under 5mph, especially when turning lock-lock out the garage, leaving T-junctions & going slowly at roundabouts where the LSD engages, requiring slight change in driving habit.

5-30mph the steering weight felt normal.

at high speed the weight feels light, very responsive feedback during turn-in (great on track) but during mid-corner the wheel starts to feel slightly heavy under the cornering forces, especially when accelerating & the LSD locks up.

she also feels rather nippy.
dunno if it's the conditions, placebo effect, reduced weight or less hydraulic drag from the deleted power steering pump providing more HP to the wheels :unsure:
I'll be curious to see if this also improves mpg too.


I always apply the “KISS Factor” & sought out & bought keep fit manual steering K11s, as its more reliable with less unnecessary complexity to go wrong in an old banger. :D
 
I didn't like how far back the steering rack sat which makes the inner tie-rod lean forward alot and this limits the angle of the rod to the inside hub during full steering lock before it binds

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Redesigned the mount inserts to seat the rack at the original distance from the bulkhead

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The drivers mount, which supports all the lateral forces of the rack, was too loose so I modified it with a tighter fit on the bracket & a gap to squeeze the rack tightly

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Test fit on the rack

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Installed

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Here you see the tie-rod angle during full-lock, shifted more forward so it doesn't bind as much

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The next issue is the outer tie-rod end.
When sitting level, the rose-joint only has just enough clearance to reach the full 2.8 turns lock-lock steering

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But when the inside wheel is at full droop (ie intense steering at a slalom course), the joint runs out of movement & binds up, potentially damaging it or limiting the steering to 2 turns lock-lock

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Hub can't reach full lock-lock

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So I'll need to machine the rose-joint spacers to give more clearance.

Neatened up the throttle cable & wiring layout

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2024-09-04 Replace Broken Radiator Fan

Yesterday I spotted the radiator fan support was broken 🤔
No idea how it happened, maybe something on the engine hit it, probably from the hard two launches recently at Santapod?

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So I visited Jack for a spare fan and saw the later facelift fans appear more efficient & stronger.
The preface has 5 thin yellow blades while the newer fan has 6 curved blades with integrated shroud to improve efficiency (helps pull air through a denser radiator core at higher pressure?)

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facelift fan has a stiffer frame, bigger motor, heavier fan blade

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Footage of both fans running.

Old fan is lighter & spins up / spools down very quickly, spins at a slower quieter rpm & creates lots of turbulance.

The newer heavier fan has slightly more inertia so it spins up gradually and spools down very gently, it spins at a higher pitch & louder rpm to create that extra pressure with abit less turbulance at the sides

 
The old air filter shield kept slipping off the ducting and the chassis lip was denting the top

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edited & printed a new one after 12hrs 🕒

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replace old with new

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curved top now clears the chassis and the added lip around the ducting helps keep the heat shield locked on

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2mths after fitting the LSD, the gear oil definately needs changing 😅

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may as well take out the gearbox to adjust the lsd & replace input bearing
 
2024-09-07 Remove Gearbox & Rebuild LSD

While disconnecting the gearbox I noticed, ohh some of the gearbox bolts were loose :unsure: might explain the oil leak & brief cold start rough bearing noise 🫣

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Removed shafts

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Removed the box

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Check the clutch soon. gotta clean the gear oil spray off the bulkhead too 🫢

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Opening up the gearbox, most of the case bolts were loose so gotta tighten em up more next time :p

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new LSD cover holding up gr8 & shiny

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Measuring all the plates, they've barely worn at all but wasn't happy with the 0nm preload so gonna rearrange with more preload

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The preload washer hasn't shattered this time but it's been squeezed down from 3.75mm brand-new down to 3.68mm total height, resulting in some lost preload

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Rearranged it using thicker clutch plates to compress the belville washer with 44% preload 💪

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Threadlocked all the bolts to 14Nm

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To measure the LSD preload, I cut & welded a 1/2" socket onto the broken driveshaft to make an adapter tool

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It slots into the spare inner CV joints so I don't have to cut & destroy them for a tool

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Now I can clamp one inner joint on the vice,
insert the LSD,
insert the other inner joint on top,
& then attach my torque wrench with the adapter shaft to measure the preload in both directions 😎

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Giving the LSD 44% of preload may have been overkill cos considering this 1-sided diff is very direction biased,
when I spin it clockwise (simulating turning left) we have a preload torque of 25nm,
but once I spin it counter-clockwise (turning right) the LSD ramp wedges & locks up solid immediately well beyond my 200nm torque wrench limit lol.

Safe to say the wheel will be skipping along the floor with hard steering every time I leave the back alley garage with tight right turns 😨🫣:poop:
 
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2024-09-08 Tighten Gear Selector Mechanism

Next issue to fix is the gear selector mechanism which has a noticable amount of side-side play when in-gear, which contributes to some sloppy feeling engagement & rattling gear-stick

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You can see in the footage the 1mm of play in the whole thing as I wriggle the selector



To remove the selector, I punch out the 3mm & 5mm roll-pins

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Selector shaft removed

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Checking the selector finger closely, the finger is 5.65mm wide but the biggest cause is the swinging selector mechanism which has a massive gap of upto 6.50mm due to how loose they're riveted together

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The selector finger & the sliding follower has a gap of 0.46mm and that limits how much I can widen the finger

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So I add a dab of weld

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Carefully file it down to the new 6.20mm thickness

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Now you see how close it slides 😎

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Selecting 1st/2nd you can see the gap is much tighter

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But in the other gears, it's actually the loosely riveted swinging mechanism above which is letting it down.
overall it feels much more precise than before.



While here, I'll replace the input shaft bearing too

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Replace the input seal & driveshaft seals

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Gearbox reassembled, tightened the casing to 17nm

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Gearbox fitted & filled with 3L fresh oil

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Went out to test the new setup



Initially leaving the garage, the steering is still heavy & LSD stutter slightly cos it needs a warm up to circulate the fresh fluids throughout the clutch plates.
But the moment I went down my street the biggest difference I notice now with 44% preload is that the LSD engagement is really progressive & quiet with almost no chatter 😃

Previously it used to have very low preload, which made it jump immediately straight up the 80% ramp, locking the plates very hard and the unsecured plates just chattered/shaked loudly.

It's abit counter-intuative but it seems the tighter preload of the belville washer keeps all the clutch plates secure under constant pressure and stops them from vibrating around loosely, which also stops the loud chatter.
The high preload also keeps the side-gear cross-pins seated deeper within the LSD 80%/30% ramps, this means it has a more progressive, smooth & consistant ramp operation without the sudden 'snap' when I lift throttle mid-corner. :cool:

Finally the modified gear selector mechanism has helped stop the gear stick from shaking around while cruising (y)
 
2024-09-14 Replace Peugeot 307 Brakes

The old brakes on the Peugeot was really rusty, scored, worn out, weak & needed replacing badly

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These silly tiny torx screws on peugeots are soo annoying at rounding :rolleyes:

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So welded nuts onto the ends 😅

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Fresh, smooth & working brakes on all 4 wheels (y):cool:

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2024-09-13 Replace Throttle Cable

The old throttle cable was slightly sticky & needed replacing

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Machined the crimped outer cable off the threaded cable adjuster so I can re-use it

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Assembled with new bicycle brake cable

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This dremel chuck is bolted onto the throttle pedal for holding the inner cable

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feed the new cable through the hole, trim to length

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Insert a bolt within the dremel chuck to clamp onto the inner cable

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Routed the outer cable at a smoother path :cool:

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The new throttle cable is definately a lot more slippery, making the engine feel more sensitive, lively & responsive to the slightest touch (y) 😎

After few miles of running the rebuilt LSD I tested the preloads by lifting the right wheel and spinning it forwards/backwards to simulate turning left/right.

When gear oil is cold & thick:
- Turning left, preload is still at 25Nm,
- Turning right, it immediately locks up beyond 200Nm.
Same values as when I tested it on the bench cold.

Once gear oil is warmed up & thinner:
Dynamic vs static friction on the plates come into play at influencing how much the ramps lock up:

- Turning left above 5mph, the plates are sliding under a low dynamic friction only forced by the belville preload washer & no ramp engagement, giving a smooth 25Nm,
- Turning left very slowly below 5mph, oil is squeezed out of the plates, which begins to grab & stutter very lightly with a higher static friction, giving a jittery 30Nm,

- Turning left to right immediately above 5mph in neutral, the plates are still sliding under a lower dynamic friction, oil still lubricating inbetween each plate under the force of the belville preload washer, which also helps to keep the side-gear cross-pin firmly seated deep on the LSD drive ramp, therefore providing minimal ramp engagement and giving a smooth approx 30Nm,
- Turning right slowly below 5mph (ie T-junctions, 3-point turns, leaving my garage), the plates begin to stop sliding, oil is squeezed out of the plate surfaces, making them grip/lock together with higher static friction, which causes the cross-pin to wedge up the LSD ramp, applying more clamping force, locking the plates with even more static friction etc making it all lock-up & stutter loudly beyond 200Nm.
 
2024-09-16 Tie-Rod End Spacer Correction

During full suspension droop the custom tie-rod ends tend to jam-up prematurely, due to the old spacers made too bluntly, which can limit the steering down to only 2-turns lock-lock & potentially damage itself if eg the inside wheel drops down a hole during a hard tight turn.

So I remachined a new spacer with more clearance & angle to give the joint more space to swivel freely without fouling.

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Can see the old joint was fouling with a limited 30deg of swivel whereas the slimmer spacer gives it 40deg of range.

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Old spacers were too blunt

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Machined new spacers from M12 nuts with a thinner deeper middle section and a 45deg relief

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Previously only reached 2-turns of steering whereas now it can reach a full 2.75-turns lock-lock no problem (y)

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2024-09-22 Non-PAS Tensioner

To delete the PAS pump for my manual-rack setup (non-PAS tensioners are rare or ££), I made this new belt tensioner

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Mounts behind the engine

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Using parts off the old PAS belt tensioner as the adjuster

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Pulley moves in/out like this

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Just ordered a shorter 4pk611 belt
 
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Thumbs up for all the info you have on the k11!

I would like to pick ur brain about something.. i have a bc racing br ra coilover set, saw you have the same one but with 5kg front 4kg back, how does this hold up against the v1 6kg front 3kg back?

I have a s20de+t swapped stripped k11 also with the br ra set currently on 7kg front spring and 5kg back springs with shorter back dampers this because i wanted to go low low, now that i am over that thinking of putting the original dampers back on , i would like some better handeling, in stead of doing just dragraces, what would you reckon with the heavier front and empty back for kind of springs to go to? i was thinking of getting the back to stock 3kg springs, but the front i am still thinkering about.. hope you could give me some insight on that since you do/did track days.

Sorry if something like this is allready asked but so many pages haha.
 
Thumbs up for all the info you have on the k11!

I would like to pick ur brain about something.. i have a bc racing br ra coilover set, saw you have the same one but with 5kg front 4kg back, how does this hold up against the v1 6kg front 3kg back?

I have a s20de+t swapped stripped k11 also with the br ra set currently on 7kg front spring and 5kg back springs with shorter back dampers this because i wanted to go low low, now that i am over that thinking of putting the original dampers back on , i would like some better handeling, in stead of doing just dragraces, what would you reckon with the heavier front and empty back for kind of springs to go to? i was thinking of getting the back to stock 3kg springs, but the front i am still thinkering about.. hope you could give me some insight on that since you do/did track days.

Sorry if something like this is allready asked but so many pages haha.
thanks m8 (y)

The dampening of the BR is soo much better than the V1.
BR with 5/4kg springs gives a firmer ride & less roll/pitch & progressive handling.
the old V1 with 4/3kg springs was comfy & very progressive cornering feel, good grip but leaned/tri-pods too much.
V1 with 6/3kg springs power-understeered on exit too much & lost time. so with stiffer spring rate it gets more sensitive, lose traction & time.
I'd only stiffen the spring rate if the suspension is bottoming out/rubbing on bump stop too often, especially if lowered too much with less bump travel or have a heavy sr20 lump.

A key note with lowered cars & heavier engine on track, the standard suspension geometry would be well-out. the front roll-center too low, high CG of the sr20 lump, making it roll & bump-steer badly in corner.

Before going stiffer springs & swaybar, which is abit of a band-aid although compromising on traction, my recommended next step is to correct the roll-center & bump-steer (extended lower BJ & arms, tie-rod bump-steer mod) to reduce the overall body-roll force & improve steering turn-in too.

Rear end is soo light already, 3kg spring is fine.

Proper X-brace at the back (bolted onto seat belt mounts) & front lower brace really helps reduce chassis flex to sharpen steering response.
 
2024-10-02 Correct Water Pump Belt

4PK611 belt was too long,
4PK595 was abit too short

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Ordered a 4PK600, which fits perfectly

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Removed the remaining PAS pump & tensioner

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The 4PK600 fits snug and no need for tensioner either since the water pump doesn't require much torque to run, so now there's less parts to go wrong/wear out and maybe reduced drag too

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The old dashboard cusion might be loose & buzzing

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so taped it up for now

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The alternator wiring seemed too tight after moving the alternator lower & closer

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I simply moved it lower down

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Noticed the screenwash tube tends to shake at certain rpm & the wideband controller has been roughly ziptied onto it for yrs 🙈

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Printed a new mount for the wideband & a little cap for the wash bottle

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Fill tube removed & bunged, inserted rivnuts for the new mount

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Wideband controller mounted solid to the chassis

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2024-10-26 North East Autoshow Darlington

Washed the car ready for the last show of the year

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Met up with TeamWhiteCustoms group in Darlington

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Arrived at the darlington football stadium

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During the show I changed the flavour of the Pringles intake 😅

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Spotted the only K10 in the show

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& a little Cherry

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All gathering to exit the show at 3pm

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2024-10-27 Replace Peugeot Silencer

The old silencer on the peugeot rusted off again so I brought another cheap box off ebay.

It looked slightly different to the photo, useing the usual cheap hanger strapped in the middle (rather than welded on shown in the photo),
& the diesel exhaust is bigger than petrol :rolleyes:

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petrol has a 43mm pipe
diesel uses 60mm pipe

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silencer is same dimensions but bigger plumbing.
instead of the hassle of posting it back & buy another one £15 more, I'm simply gonna modify this to fit

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old pipe easily snaps off, gonna re-use this fitting

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chopped the large end off

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have to make this 43mm end fit within a 60mm hole :unsure:

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Afew pie cuts to taper the size down

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welded on

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also extended these short hangers

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exhaust fitted & fixed

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2024-11-02 Radiator Fin Straightening Comb

The old radiator fins are slightly covered in bugs

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& some on the back are bent, not good for efficiency especially once it's turboed

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so I printed this precise 1.4mm teethed mini comb 🤏

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works great at straightening each fin

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2020-2024 Redesign Exhaust Manifold

From 2011-2019 my old turbo setup had this crude layout with lots of tight bends & factory unequal length manifold, not great for flow or efficiency

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Since the turbo setup last blew up in 2018 I've been running this factory NA manifold that's been opened up to 2.25"

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Instead of using the same inefficient turbo manifold & layout, I decided it's time to redesign the whole package for improved flow.
So for the past 4 yrs I've been trying to redesign the manifold with the goal of:
-equal length runners for consistant equal exhaust pulses at the collector for better turbo spool-up & scavenging,
-short runners to try keep the exhaust gas hot & position turbo close to the engine away from the alternator & radiator,
-easy to make at home with current tools.

I had almost 100 designs ranging from:

- Unequal Length Log Manifold

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- 421 headers

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- 431 headers

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- 4-1 Ram-Head

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- 4-1 Long Looping Headers

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- 4-1 Compact Short Headers

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- 4-1 Long Headers

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🥴
 
2024-10-30 Equal Length 4-1 Turbo Exhaust Header

This was the latest chosen design #97 which closely met my design goals.
Has equal length runners, compact, doesn't require many U-bends to make, simple angle cuts, few welds to do compared to joining hundreds of pie-cuts

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The turbo exit elbow barely clears the radiator & front engine mount while maintaining a smooth large 2.25" bend

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The runners clear the front slam panel & bonnet

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The turbo intake is right above the alternator leading over to the cooler right-side of the bay where the washer bottle filler is (I'll adapt a cold intake duct here)

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Before the turbo & spare engine is rebuilt/fitted, I'll be running the new manifold in NA like this with the new sports cat sitting up close to hopefully help with MOT emissions

manifold 97 09.jpg


Designed this simple jig to hold the T2 flange while constructing the complex runners

manifold 97 02.jpg
 
Last edited:
2024-11-01 Fabricate New Turbo Manifold

Cleaned up these 38mm steel U-bends I had in storage

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Marked out the 70/90/180deg bends required

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I'll need to adapt this band saw to hold & cut the precise bends

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Printed these jigs

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Added an extra screw hole to the band saw

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Now I can cut each bend

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All 4 runners chopped, and now the most difficult part is merging them all into a collector

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I carefully marked the layout of each precise complex cut on the pipes

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Printed this jig to hold the flange into position while reconstructing the runners

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Getting all 4 curvy cuts to line up was quite difficult, frustrating & fiddly 🤯

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I may have cut too much material off the complex join and manually filing/grinding it to fit wasn't working, so thought fookit lets join it & deal with the slightly wrong angles.

Tacked the merge collector together, runner #1 & 4 are pointing up too much, they should be pointing flat

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With the runners pointing up, there's a large gap near the flange

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Managed to move #1 runner closer together but I had to add a short section to #4 runner 😕

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Split it apart to weld around each runner.
Originally I wanted to neatly TIG it but somehow it wasn't working properly with the gas-lens tip so I MIG welded instead, which was better for filling large gaps, consistant & very familar/reliable

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Welded the outer runners to the inner runners while I still had good access to smooth the inside merge

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Tried to reattach both runners together onto the flanges but due to warpage, it was hard to line up without this gap in the middle, which I eventually had to fill up using the MIG

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Completed MIG welding the whole manifold. MIG ain't neat & lots of spatter so may need smoothing using the TIG 🤔

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Oooh that looks satisfying & cool 😎

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Just enough gap from the turbo & engine area

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The silicone join at the compressor outlet might be abit toasty near the T2 flange 🥵

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Turbine outlet sitting level for the 2.25" elbow

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Can just barely squeeze the dip-stick inbetween these runners 🤏

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Found the gas-lens was once again faulty/blocked whereas the regular pink nozzles worked fine :rolleyes:

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I got carried away trying to smooth out every rough MIG weld with the TIG, forgetting I was putting too much heat/warpage on the runners until I realised the ends of the flange warped badly by 5mm 🤬😨

That's gonna be difficult to sand flat or I'd have to start over with a new flange?

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After chatting with Jack, I decided the 1-piece flange & runners where straining each other, so I separated each flange & correct the warped #4 flange

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Bolted onto the head, using it as a straight jig

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Welded the warped flange back onto the runner

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That's a little better to belt sand it flat later

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Blanked off the ports to leak test the welds

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Blowing air inside whilst submerged, there were afew leaks around the 10mm thick flange 😤

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Trying to TIG weld up every pin hole leak & retesting it only to find more leaks was seriously frustrating & putting too much heat into the flange

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welding it up from the outside wasn't working so I TIG welded it from the inside of the port and that's finally sealed it up

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Last step is to belt sand it flat & paint.

As a 1st attempt it definately ain't perfect, so many things went wrong, it tested my patience, hope I don't have to go through it all again lol but suppose it's part of building experience.

Curious to see if it works out 🤞

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Ideally I wanted a long bench sander to flatten the whole flange evenly but they cost over £200!

Next choice is the old portable belt sander, some of them range from £50-180 fancy features (which I dont care about) but for this one-off task I managed to find a cheapo sander in argos for £33 😁

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It only has a 76x130mm flat base so I'll flatten the long flange bit by bit, checking with the straight rule

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Compared to how I used to manually hand sand over a glass plate, this is much quicker 🤪 but it still takes awhile to remove over 1mm of warpage.

The ends of the flange where it's most warped will take ages to flatten but I think I'll just machine enough off the overall area until it barely covers the gasket surfaces

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Turbo flange was much easier to flatten :cool:

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Tday removed the current standard cast manifold

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Old vs new manifold

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This catch can / shield plate was in the way so needs removing. I'll make a new shield & relocate the catch cans at some point :unsure:

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Fitted the new header

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Refined the downpipe to include a V-band join & position the wideband sensor to the side for easy access & good flow

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Marked where to cut on the downpipe

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I can now weld the V-band on at the correct angle

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Joining the new cat onto the T2 flange required a 9 deg slope cut, so I marked it using some paper drawing

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Chopped

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For welding access I attached the wideband sensor nut on first

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& then welded the flange & V-band onto the ends

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All installed :cool::cool:

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It looks sooo good 👌

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Whilst fitting the header I also test fitted the turbo inside the bay 😛

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The alternator cable & dipstick barely clears the compressor

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dipstick angle & the compressor-to-wastegate line may need some adjustment

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After dinner I fired up the engine 🤞 and she starts very immediately/freely.
No leaks anywhere.
As the header heats up, the VHT paint obviously smoking/curing for afew mins.
Exhaust sounds a little smoother, quieter & doesn't resonate the house windows as much as compared to the standard manifold.
AFR throughout idle/cruising/WOT were the same so map won't need much tweaking which is a relief.
Driving her at night, the low-end torque seems kinda the same, mid-high end felt very slightly better & smoother delivery (dunno if that's the cool night air too 🤔)
Something noticably different is a resonating exhaust drone at exactly 3k rpm (cruising at 70)
 
This morning I saw the VHT paint over the grey primer has began to all crack/peel off 😬🙈

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Almost all peeled off from the heat tonight.
Guess I'll have to wirebrush it all off and spray the silver paint directly onto steel this time as mentioned on the spray can 😅

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Recorded a cheeky little rev with her new exhaust today 😛
The tone is still the same but very slightly sporty rushing gas noise at the low end :unsure:



On the way home her gear stick mount suddenly snapped off along the slip road while launching hard 😨
Managed to barely select a gear & nurse her home few hours before tonights car meet 🙈

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Looks like it was too thin weak, few stress points near the screws and the hollow in-fill didn't help

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Quickly printed a slightly thicker mount in 40mins

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Enough to make the car meet 😁

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Now that I ripped off that rubber dust boot, I'll redesign a more chunky stronger pivot mount next
 
2024-11-15 Print Stronger Gear Stick Mount

After snapping the gearstick mount & ditching the rubber dust boot, I designed a much beefier mount

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Uses the same ball socket insert sized to fit snug without binding

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The green plate is pushed over the hex screws to lock & prevent them loosening

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Printed

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& feels much more solid :cool:

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2024-11-15 Repainted New Manifold

It seems the grey acrylic primer I applied by mistake (thinking it would've helped adhesion) turned to dust from being cooked by the heat therefore the hard cured VHT paint had nothing to cling onto and all peeled off 😅
(well it did say on the spraycan no primer needed lol)

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Wirebrushed & cleaned the mess off

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& sprayed silver VHT directly onto steel this time, hope it works better 🤞

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Fitted the repainted manifold.

Made this shield for the front panel out of spare aluminium (similar to factory panel) to protect the engine/manifold/turbo from being blasted with weather (reduce rust), debris, cold air (keep exhaust hot for turbo) & help divert air through the radiator instead

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Enough room to fit & protect the turbo layout.
The alloy shield also won't rust away from being blasted by incoming air.

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Warmed up the engine, painted manifold smoking/curing again but for much shorter period.
Went for a blast around town to cook the VHT paint, once home & cooled down the VHT paint is still intact & cured correctly.
Lesson learnt is acrylic primer ain't heat resistant 😅

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Covered the front of the panel shield with black vinyl to stop the bare aluminium shining through the grills 🙈
& form a protective layer from incoming debris & weather

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Some stainless O2 sensor nuts also arrived for when I make the turbo downpipe

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Last edited:
2024-11-16 Micra Cooling System Warm Up Sequence

Jack was having issues with his micra taking forever to warm up whereas mine heats up in few mins.
So I measured some temps to show how the system normally heats up.

Labelled some of the essential hoses I'll be feeling for.

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Heater dial is turned to full cold so the heater matrix valve is closed allowing the engine to warmup quicker.
Coolant temp starting at 20deg, I fire up the engine & let it idle.

#After 3 mins:
Coolant: 45C
Heater Feed: Warming up
Heater Return: Cold
Rad Top Hose: Cold
Rad Core: Cold

#After 6 mins:
Coolant: 63C
Heater Feed: Warming up
Heater Return: Cold
Rad Top Hose: Warming up
Rad Core: Cold

#After 9 mins:
Coolant: 70C
Heater Feed: Hot
Heater Return: Cold
Rad Top Hose: Warming up
Rad Core: Cold

#After 13 mins:
Coolant: 80C
Heater Feed: Hot
Heater Return: Warming up
Rad Top Hose: Warming up
Rad Core: Cold

#After 15 mins:
Coolant: 83C
Heater Feed: Hot
Heater Return: Warming up
Rad Top Hose: Hot
Rad Core: Hot

Thermostat valve cracks open at 82C,
Hot coolant from engine enters into the radiator core,
The stone cold coolant
from the radiator core & return hose joins the cooling system,
Drops the coolant temp down to 77C

#After 16mins:
Coolant climbs back to 82C and stays there while the radiator core keeps getting hotter.

Eventually the radiator core is saturated with too much heat it cannot statically radiate away fast enough,
So the coolant temp rises towards 95C,

Once the ECU sensor gets over 95C it spins the cooling fan to cool the radiator core, bringing temps back down
 
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