pollyp
Club Member
recently noticed that the printers heated bed was slightly twisted at the far end where it's only supported by 1 of the 3 mounts, making it difficult to ensure a flat platform across the whole bed.
decided to drill two new holes so it can be adjusted at 4 corner points.
but there's no existing schematics about the makibox heated bed circuit layout hidden under the steel plate,
I'm just hoping all the circuit routes within the mounting holes and I could dril around the outside.
drilled two new holes in the bed & moving frame
applied an insulator under the bed to help reduce heat up time
OK reconnected it all up, power on and erm nothing, controller is blank and power adapter light is blinking, Oh ohh this ain't good.
is it a short? I'm screwed if the beds broken.
unplugged the heated bed and the rest of the XYZ motors are working again, phew I didn't blow the controller, good thing it has some shorting protection.
Ah pants, the heater circuit must've gone under where I've drilled and shorted out :/
Right, time to split the stainless plate off the PCB heater board. it was tricky with alot of razor blades but eventually separated the high temp adhesive tape without damaging / bending the board much
and yeah I drilled straight through the circuit
so here's the circuit layout
red = 12v feed towards center
blue = ground feed
green box = glass bed
gonna have to reroute the circuit to bypass the conflicting new screw holes and disable part of the heater element outside the glass bed to prevent it overheating.
so gonna reconnect the areas marked in yellow
exposed the copper tracks
connected some areas with conductive paint
connected this crucial 12v feed overhead the ground feed by soldering afew strands of copper wire
the flat areas under the glass bed connected with conductive paint. I also grinded any remaining copper tracks away from the screw holes so it doesn't short out through the metal chassis
removed copper backing away from the screw holes underneath
fibre washers insulating between the screws and PCB
another issue is the bed. I could either:
- bond the stainless plate back onto the PCB heater (temporarily with some double sided high temp tape or permanently with epoxy thermal paste) to spread the heat and able to bend the metal flat then clamp the glass on top, but heater still has to slowly heatup both the steel & glass bed.
- or simply clamp the already flat glass onto the PCB heater for fast heatup but air gaps may affect heat distribution.
decided it's easier & better to just clamp the glass on top.
finally found 4 tiny binder clips to secure the bed from the corners.
the heated bed finally works and works really well.
I'm able to adjust all 4 corners completely even flat (there are some gaps between the flat glass & the PCB cos the PCB has bent slightly after I pryed it off the stainless plate but it's a minor issue) and by clamping the glass directly onto the PCB heater, the heatup has reduced from 7min down to just 4min
happy with the improvement.
decided to drill two new holes so it can be adjusted at 4 corner points.
but there's no existing schematics about the makibox heated bed circuit layout hidden under the steel plate,
I'm just hoping all the circuit routes within the mounting holes and I could dril around the outside.
drilled two new holes in the bed & moving frame
applied an insulator under the bed to help reduce heat up time
OK reconnected it all up, power on and erm nothing, controller is blank and power adapter light is blinking, Oh ohh this ain't good.
is it a short? I'm screwed if the beds broken.
unplugged the heated bed and the rest of the XYZ motors are working again, phew I didn't blow the controller, good thing it has some shorting protection.
Ah pants, the heater circuit must've gone under where I've drilled and shorted out :/
Right, time to split the stainless plate off the PCB heater board. it was tricky with alot of razor blades but eventually separated the high temp adhesive tape without damaging / bending the board much
and yeah I drilled straight through the circuit
so here's the circuit layout
red = 12v feed towards center
blue = ground feed
green box = glass bed
gonna have to reroute the circuit to bypass the conflicting new screw holes and disable part of the heater element outside the glass bed to prevent it overheating.
so gonna reconnect the areas marked in yellow
exposed the copper tracks
connected some areas with conductive paint
connected this crucial 12v feed overhead the ground feed by soldering afew strands of copper wire
the flat areas under the glass bed connected with conductive paint. I also grinded any remaining copper tracks away from the screw holes so it doesn't short out through the metal chassis
removed copper backing away from the screw holes underneath
fibre washers insulating between the screws and PCB
another issue is the bed. I could either:
- bond the stainless plate back onto the PCB heater (temporarily with some double sided high temp tape or permanently with epoxy thermal paste) to spread the heat and able to bend the metal flat then clamp the glass on top, but heater still has to slowly heatup both the steel & glass bed.
- or simply clamp the already flat glass onto the PCB heater for fast heatup but air gaps may affect heat distribution.
decided it's easier & better to just clamp the glass on top.
finally found 4 tiny binder clips to secure the bed from the corners.
the heated bed finally works and works really well.
I'm able to adjust all 4 corners completely even flat (there are some gaps between the flat glass & the PCB cos the PCB has bent slightly after I pryed it off the stainless plate but it's a minor issue) and by clamping the glass directly onto the PCB heater, the heatup has reduced from 7min down to just 4min
happy with the improvement.