pollyp
Club Member
little update.
that annoying plastic squeak/shuffle noise has returned, even after I tightened all the panel screws and even screwed the parcelshelf onto the plastic base itself.
mpg seem to have improved after swapping from the old clogged air filter to a newer one but oil consumption is still bad. driving 240m to a long meeting and back its gone from 3/4 dipstick to bottom low :/
oil was black so changed oil & filter.
the random warm exhaust misfire cough was still there. tried gapping the plugs to 1.0mm to no effect.
replaced the old plugs with new ones
still coughs
cyl 1-3 are 1/4 damp while cyl4 is still all damp, notice the sooty 4th plug, I think that's where it's misfiring.
when the warm engine has stopped for afew secs so things are slightly cooler and start the engine, the first few secs are firing smoothly.
but after 10sec it begins to randomly misfire.
it always did this with both the forged and stock engine block. when I swap over to a stock NA setup with stock injectors etc for MOT it never randomly misfires.
so overall I'm suspecting it could be a dirty/leaky sr20 injector during high vacuum idle?
I'm thinking of adding a tank of injector cleaner, what ya'll think. which brand is recommended or will ones from halfords do?
that annoying plastic squeak/shuffle noise has returned, even after I tightened all the panel screws and even screwed the parcelshelf onto the plastic base itself.
mpg seem to have improved after swapping from the old clogged air filter to a newer one but oil consumption is still bad. driving 240m to a long meeting and back its gone from 3/4 dipstick to bottom low :/
oil was black so changed oil & filter.
the random warm exhaust misfire cough was still there. tried gapping the plugs to 1.0mm to no effect.
replaced the old plugs with new ones
still coughs
cyl 1-3 are 1/4 damp while cyl4 is still all damp, notice the sooty 4th plug, I think that's where it's misfiring.
when the warm engine has stopped for afew secs so things are slightly cooler and start the engine, the first few secs are firing smoothly.
but after 10sec it begins to randomly misfire.
it always did this with both the forged and stock engine block. when I swap over to a stock NA setup with stock injectors etc for MOT it never randomly misfires.
so overall I'm suspecting it could be a dirty/leaky sr20 injector during high vacuum idle?
I'm thinking of adding a tank of injector cleaner, what ya'll think. which brand is recommended or will ones from halfords do?